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オリジナル投稿者: smsoftware

タイトル:

Short shift and turn.

テキスト:

Navibot sr8855 after repair of FET tranzistors for  brush have bad mooving - navigation.

From the beginning it worked well and after some time was problem in navigation.

It looks like that: move 20-30cm stop and go back about 3cm, turn 90st. and repeat.

Sometimes work good for 1 minute and then again fail to this state.

I try test mod and all sensors look fine, motors are OK too.

デバイス:

Samsung NaviBot SR8855

ステータス:

open