オリジナル投稿者: smsoftware
タイトル:
Short shift and turn.
テキスト:
Navibot sr8855 after repair of FET tranzistors for brush have bad mooving - navigation. From the beginning it worked well and after some time was problem in navigation. It looks like that: move 20-30cm stop and go back about 3cm, turn 90st. and repeat. Sometimes work good for 1 minute and then again fail to this state. I try test mod and all sensors look fine, motors are OK too.
デバイス:
Samsung NaviBot SR8855
ステータス:
open